NC23 racebike engine failure
Posted: Mon Jun 08, 2009 11:55 pm
Took my NC23 to the track on Sunday for the first time. Was a having a ball getting use to it, corner and exit speeds gps logged almost as quick as my gixxer thou after only 2 sessions.
Anyways, 3rd session the engine let go. On the bike sounded like grinding gears or something slipping in the gear box, i didn't really think it was engine initially, till I turned around to see huge amount of smoke come out the pipe. Engine was still running but definately down on power some. I just upped to 6th gear and cruised around the outer edge of the track back to the pits (maybe i should have shut it off then and there? oh well lol).
I'm guessing maybe some valve to piston action?
Having been warned about over reving, my shift points were at 14,000, I don't think I was downshiftting too hard (all a big adjustment coming off an 06 gixxer 1k)
However, only moments before it shat, was on the front straight and it did pop out of gear. Defiantely wasn't a miss select (maybe just not in hard enuf) but full noise/throttle it got a fault neutral, tho honestly I can't see how such a short incident can kill a motor? (never had such issues with the year & years of suzuki's i've tortured lol).
The motor was like 2 track days old, topend and bottom end, had head and valve work etc (apparently) .
Will drop it off and pull the head to see some more when i get a chance. So annoying, 30min of riding since purchase
Anyways, 3rd session the engine let go. On the bike sounded like grinding gears or something slipping in the gear box, i didn't really think it was engine initially, till I turned around to see huge amount of smoke come out the pipe. Engine was still running but definately down on power some. I just upped to 6th gear and cruised around the outer edge of the track back to the pits (maybe i should have shut it off then and there? oh well lol).
I'm guessing maybe some valve to piston action?
Having been warned about over reving, my shift points were at 14,000, I don't think I was downshiftting too hard (all a big adjustment coming off an 06 gixxer 1k)
However, only moments before it shat, was on the front straight and it did pop out of gear. Defiantely wasn't a miss select (maybe just not in hard enuf) but full noise/throttle it got a fault neutral, tho honestly I can't see how such a short incident can kill a motor? (never had such issues with the year & years of suzuki's i've tortured lol).
The motor was like 2 track days old, topend and bottom end, had head and valve work etc (apparently) .
Will drop it off and pull the head to see some more when i get a chance. So annoying, 30min of riding since purchase
