Well this issue continues to drive me insane.
Some experiments tonight,
wound out pilot screws 1/8th to 1 6/8ths per advise on here that doing so will lean it out. It ran worse. fire from exhaust on idle + dies with choke.
From here wound them in one half turn, to 1 2/8ths.. Bike seemed to run a bit better, as in idle adjustment screw seems to need to be wound on less to keep it running, still dies with choke.
Tried in another half turn, no change, still dies with choke burping a little fire at idle.
From here went overboard. 2 1/4 out. creating theoretical very lean. No difference. Dies with choke immediately and with only a small amount.
went out 1/2, 2 3/4, no change
went out again, 3 1/4 (!!!!). no change.
All experiments were tried with and without the airbox/filter, with no difference to any result. No result is notice if i hold my hands over the trumpets and no vacuum is felt, so the idle air must be fine.
After experiments i pulled one of the plugs, and predictably it was wet and looked like shit.
As it came out:
http://imgur.com/SlbK47T Wiped down:
http://imgur.com/igHQYjM
carbon on them seems to come off with my fingernail. next step is to pull em all and clean em. Plugs are only 400kms old so buying new ones would piss me off, especially if they didnt fix the issue.
So, from the fact that wildly fucking with the pilot screw didnt affect how the bike idled very much, it would suggest that the pilot screws are missing parts or are blocked. Which they are not, and which cant be the case, as only a week ago i had them apart and cleaned out with degreaser and an air compressor.
Which leaves float heights... which is a completely subjective measurement, leaning against the knob on the valve, slightly
slightly compressing it, making sure the float is seated, gives roughly the same result as simply having the carbs upside down, this measurement with a steel rule and vernier calipers is correct at 12~13mm.. if the knob on the needle is not at all touched the measurment could be ~14... which would make it leaner?!?!!
Just removed the carbs and pulled out all the pilot screws to confirm that no parts are missing or the needles broken off. Will take in to work with the air compressor again tomorrow, focusing on the pilot circuit. To clarify, going in reverse, this circuit goes from a hole in the carb near the butterfly, up through the pilot screws needle valve to one of the 3 brass fittings in top of the carb, with no fuel added along the way? (i just want to know where i should be focussing on unblocking)
Thinking about this seems like such a stretch, as it is so odd that it would be blocked equally on all 4, but if the shit running was caused by the plugs and the pilot circuit had no fault, and if the pilot screw setting is as sensitive as i am led to believe.. then wouldnt it have eventually died when i wound it to the extreme values above?..